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J.A. Fay and Egan Model 316 12 Inch Jointer Restoration. Origins · Purchasing · Relocation · Repair · Restoration
Click here for .pdf version of J.A. Fay & Egan, Co. catalog entry.
In 1869 the Illinois General Assembly appropriated funds for the location and establishment of the Northern Illinois Hospital
and Asylum for the Insane. Nine commissioners were appointed by the Governor to choose a suitable site on which to
locate the institution. After selection of a site in Elgin a board of three trustees, appointed by the Governor, was
empowered to supervise planning and construction, choose a superintendent, and operate the institution, subject to
inspection by the Board of State Commissioners of Public Charities. The jointer had been used to clean up raw wood for everything produced in the woodworking shop. This includes all of the moldings made for the mental health center. The jointer came with a large wood box of molding knives that the chief said were always with the jointer. No one knows for sure if they were used on the jointer, but he had the feeling they were. The last place the jointer had been was in the mason's shed setting on its side on a dirt floor. He was not sure how the jointer was cracked, but thinks it may have happened in the move to the auction in Springfield.
Purchasing.
Upon first inspection of the beast, I noticed the the rabbeting arm had been broken off, and that there was a substantial crack on the in-feed sled casting as viewed from the underside.
That evening I researched the jointer and determined that I needed this machine (necessity always being my first justification) and that I could bring it back to life (I know 'righty-tighty lefty-loosy' has to do with screws and bolts), and, I could afford it (credit cards are not all maxed out yet). So, with the justification that a new 12 inch jointer of such quality could go for many thousands of dollars and that I really needed one, I was willing to spend quite a bit for this hunk of broken cast iron. On Wednesday, January 19, 2005, I took some time off work and went to the auction. Of course if you are waiting for one individual item, it will be one the the last to go and so was the case for this jointer. During the wait, I met several old timers interested in the jointer and talked with a few about the possibility of the large crack causing permanent damage to the in-feed table angle and so on. Anyway, I made a few new friends in the hours of wait time and have since been to their workshops to see their old iron (more about that later). When it came time for the woodworking machines, the order was everything else, then the jointer. Of course not knowing how much I would have to spend on the jointer, I let the Yates shaper and DeWalt mortiser slip by me for less than $100 each. Aarg!
Then came time for the jointer, the auctioneer started the bidding at a $1000 dollars... of course he did. When it finally was reasonably bid at $50, I started in. After a $100 there were only two of us bidding. At $200 I had the feeling the old timer was purposely running the price up... I may still have had the previous day's giddy look on my face. Finally, for $250 I had won the item. Along with the jointer came a hundred pound box of jointer knives that supposedly go with the jointer. They look like shaper knives for a large square cutter head. Also, a Westinghouse 3 phase 7.5 h.p. motor with 4 inch leather belt and shiny new set of blades for the jointer. Thanks again to Visa for making this all possible.
Relocation. One of the fork lift operators then loaded this on a borrowed single axle tilt trailer rated for 2000 lbs. I wish there had been video footage of this event. When the full weight of the machine was applied to the trailer a shriek came from from somewhere in its leaf spring suspension that made everyone move away quickly. I strapped the machine down, it seemed like the right thing to do, knowing there was no stopping this it from tipping if it got to that point. It was amazing how once turned right-side-up, the charisma of this jointer reduced grown men into giddy schoolboys. There was no lack of volunteers to help in getting the jointer up and on the trailer and strapped down.
Driving it home was as eventful as it could have been. No one pulled out in front of me or even stopped short. I guess only
having to travel 11 blocks was a bonus in this case. Of course the two sets of train tracks on the way were a bit rough. When
crossing the second set, the crossing lights and bells activated, and the crossing arm came down shortly after I
cleared their reach. I don't know whether the crossing arm or the jointer would have won that battle, but somehow I'm sure
the jointer and I would have been long gone when the police investigation began. Once home I backed the trailer down
the driveway and parked it until later. On Thursday after returning from work, I backed the trailer until it just entered the garage. I jacked up one end of the skid nearest the rear of the trailer and installed two 5 inch free turning casters. Next I removed the jack and pulled the trailer tilt pin. Thankfully we had done a good job centering the weight over the axle, I carefully lifted the front of the trailer until the rear was firmly on the ground. I didn't know whether it would slide off on its own or not, but, it didn't. I grabbed a long steel pipe I use for leverage on wrenches and cinched the jointer down the trailer and into the garage. Excellent... Next I jacked up the other end of the skid and added four more casters. My day ended with a sigh and a cold beer.
Repair
Now to get the screw fixed. Of course when presenting to a local machine shop, they seemed carefree when saying, "No
problem, we'll put it in the press and straighten it out.". I joyously went back to work and waited anxiously
for their call. Later that afternoon, I received a call from Napier and was notified that the screw broke. With a little yankee engineering, a piece of plate steel, some JB Weld and set screws I was able to reassemble the screw. I first set up a jig on my disc sander and ground the two pieces to 90º. Then I cut a 1/2" thick piece of plate steel to the dimensions of the diameter of the collar on the shaft part of the screw. I drilled and counter bored holes for set screws and attached the plate steel to the collar. Next I screwed the screw into the machine, placed the gear shaft into the sled and put the sled back on the machine. Once I got it lined up where it was supposed to ride, I jb welded the screw to the plate steel. A couple days later I went out and carefully removed the screw with newly mated shaft from the jointer. I removed the set screws and was able to drill two holes for set screws through the plate steel and into the screw. After tapping these holes very, very, very carefully, I installed my set screws, added some jb weld to the shaft side of the plate steel and reattached it with the set screws from earlier. A day or two later came the moment of truth. I put the screw back on the jointer, set the sled back in place and installed the gears. I was nervous when I tested the up and down adjustment and almost wept over the sweet ride.
Ok, one problem down, many to go. The crack was long and deep. I thought maybe someone could weld this thing back together, but
everyone said that if that slide got too hot, it could warp and would never mate perfectly again. So, I filled it full of JB
weld and tried to clamp it up. Did you guess that this wouldn't work? Well if you did, you were correct. Now I had a
lateral support that didn't keep the sled where it was supposed to. I tried chipping away at the weld, but broke the
entire piece off instead. Now for mechanized power. The large motor must have been mounted to the floor within a few feet of the machine and was totally overkill for this machine.
According to the catalog entry on this machine, the 12 inch model used a 3 h.p. motor and only the 30 inch model used the 7.5 h.p. motor. I purchased a 5 h.p. single phase 230 v motor from one of the old timers that I had met at the auction. I mounted the motor on 1/4 " plate steel and was able to just fit it under the machine. Now I had to find pulleys to drive it. Well with help from the OWWM discussion group, I realized that legitimate sheaves and pulleys are way to expensive. So, I went to a website called www.surpluscenter.com and found a cast iron double grove pulley that was perfect size to give me reasonable blade speed. I had to take the 4" leather belt pulley off of the cutter head shaft and have two grooves cut into it to match the motor pulley. For $80 double groove cutting, a $26 2-groove 9 inch motor pulley and a $25 v-belt, I had enough to test it.
I hooked up the pulleys, mounted the motor, added a belt and wired the system to my table saw switch. (don't worry, I checked the jackscrews too.) I was in the other room with the table saw when I first started the jointer. Yee haw! Hearing it fire up and sound like a big machine should was awesome. With the extensive help of Alaskan Frontiersman and OWWM.com member Dan Hall, I was able to get a Westinghouse motor starter and an Allan-Bradley pushbutton station operational. Next comes the restoration. I will try the electrolysis method on as many parts as I am able and see how it goes. |
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